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Day 140 - Dual Thrust 2 - Improvements and Measurement
Date:23rd
December 2013
Location:Workshop, NSW, Australia
Conditions:temp
25C
Team Members at Event: PK and GK.
After the static tests and flight trials
of the dual thrust rocket on
day 138, we
believed there was some room for improvement with
the performance. One of the major problems
was the blow-through effect allowing
pressurised air to escape from the boost
chamber before all the water had run out.
(Here is an example
of the loss of thrust due to
blow-through from previous experiments.) The sustain air pulse thrust also
didn't look like it was efficient due
to the internal nozzle being so far into the
boost chamber. Kind of like blowing into
your own sail. Some water was being held up
against the sides during the sustain air pulse as
well.
Another problem was the vacuum created in
the boost chamber during the sustain air pulse
causing the bottle to collapse inward.
To address these issues we extended a
narrow thin-walled tube down through the
boost nozzle. This tube weighs 9 grams.
Original configuration with
Jet Foaming spacer
New improved configuration with
Non-return valve and extension
tube
Launched with the same
Clark cable-tie launcher
Non-return valve
Extending the tube all the way down to the nozzle meant that
we would lose the water self-levelling feature of the jet
foaming spacer. So we built a non-return valve into the bottom
of the spacer so that water and air could flow up into the
sustain chamber during pressurisation.
How it works
The non-return valve is built into the adaptor that holds the
extension tube inside the spacer. We cut a "V" shaped groove around the
outside of the adaptor to house an o-ring. Small inlet holes
were drilled from the bottom into the base of the V-groove.
During pressurisation the higher pressure in the boost
chamber causes flow through the inlet holes and because the
o-ring is in a V-groove it pushes the o-ring out of the way
breaking any seal allowing the air and water to flow out from under the o-ring.
The top of the adaptor is narrower than the spacer with less
than 1mm gap all around. This allows the water and air to flow
upwards into the spacer without affecting the flow efficiency
back down the extension tube during the sustain phase.
Shortly after launch, the pressure differential between the
sustain and boost chambers switches and the water pushes the
o-ring back into the V-groove blocking the inlet holes. This
ensures that all the flow from the sustain chamber only goes
through the extension tube.
Non-return valve and extension
tube adaptor
Extension tube fitted
into the non-return valve
All the components including
the existing spacer
Fully assembled ready to be
fitted
into the boost chamber
The extension tube extends
past the end of the nozzle
Thrust Measurement
In order to do some quantitative comparisons we ran a series
of tests of the rocket on the load cell to measure the
amount of thrust generated.
We used our load cell setup for these
experiments. Because this dual thrust rocket
produces such a wide difference in peak thrust between the two
phases we had to reduce the gain on the load cell amplifier so
that we wouldn't clip the top of the boost thrust phase but on
that setting the amplitude resolution for the sustain phase
wasn't very much. At 100psi the boost peak thrust was expected
to be around 450 N (101 lbf) and during the sustain phase the
peak thrust was expected to be around 20 N (4.5 lbf). So we ran some tests where the boost phase
was completely visible and other tests where we turned up the
gain to get better amplitude resolution in the sustain phase,
but clipped the boost phase.
Experiment Setup
The extension tube had a 7mm internal diameter, which was a
little on the larger side, so we made a small plastic insert
that was glued into the bottom of the tube with a 5mm hole. This
way we could compare the performance of the previous spacer design with
the new design.
Small 5mm ID insert for the
extension
tube to reduce it from 7mm to
5mm
Extension tube fitted with
reducer.
The rocket under test had the following parameters:
Diameter: 90mm
Capacity: 6085mL
Boost nozzle: 22mm (20.86mm effective when we remove the
cross sectional area of the extension tube),
Sustain nozzle: 5mm
Configuration: 3 x spliced pairs joined with a full-bore
tornado tube on the bottom, and 18mm tornado tube at the
top.
We used 3 video cameras to record each test. The HD
camera for real-time view, the GoPro at 240fps
to film the entire rocket, and the Exilim FC100 at 210fps to
film close-ups of the boost chamber.
The release mechanism was a standard
Clark Cable-tie launcher in
order to use the full 22mm nozzle. It was attached by a
string to prevent it from impacting the ground during
launch.
Results
Preliminary Tests - 22/12/2013
The first tests with the new configuration were carried out
just mounted to the test stand (no load cell). These tests were used to check
whether the system even worked at all. Two test firings were made
with a full 7mm sustain nozzle. These tests were carried out at 100psi
(6.9 bar) and 1700mL of water.
Test #
Configuration
Water amount
(mL)
Split
Boost / Sustain
( mL / mL )
Pressure
(psi / bar)
Nozzle
Boost / Sustain (mm)
Notes
1
Extension
1700
1000 / 700
100 / 6.9
22 / 7
Good test, no blow-through evident.
2
Extension
1700
1100 / 600
100 / 6.9
22 / 7
Good test, good boost water column
Test #1
Test #2
Measurement Tests - 23/12/2013
The following tests were carried out the next day mounted to the load
cell.
Test #
Config
Water
Amount
(mL)
Split
Boost / Sustain
(mL / mL)
Pressure
(psi / bar)
Nozzle
Boost / Sustain
(mm)
Thrust curves
1
Extension
1800
1150 / 650
100 / 6.9
22 / 5
Load cell amp set to low gain to show all of the boost
phase. Second view is the zoomed in view onto the boost
phase.
2
Extension
1700
1045 / 655
100 / 6.9
22 / 5
3
Extension
1700
1100 / 600
100 / 6.9
22 / 5
Load cell amp set to high gain to show details of the
sustain phase. The boost phase is clipped.
4
Extension
1800
-
~30 / 2
22 / 5
Self launch - Invalid test
5
Extension
1800
1300 / 500
100 / 6.9
22 / 5
No o-ring test to try to help self-levelling.
6
Spacer
1800
800 / 1000
100 / 6.9
22 / 5
Looking at the sustain phase of the spacer, with
dramatic drop off at the start of the air pulse.
7
Extension
1800
1100 / 700
100 / 6.9
22 / 5
No o-ring - split water (poured half into sustain chamber)
8
Spacer
1800
800 / 1000
100 / 6.9
22 / 5
Low gain to inspect boost phase of the spacer. Second
curve is a zoomed in view.
Analysis
When looking at the spacer thrust curves
from tests #6 and #8 it is evident that
the thrust sharply drops to almost 0 at
the start of the sustain air pulse.
This coincides with the bottle collapse,
and as can be seen in the video that the
air coming out is fairly low velocity.
When we compare this against test #7 we
can see that there is the typical air
pulse tail-off like in normal water
rockets. Test #7 ends the sustain water
phase sooner because there was only
700mL in the sustain chamber compared to
1000mL in test #6. You can also see the difference in that the
boost phase for #7 was about 10% longer compared to #6 because
there was more water in the boost
chamber.
We can
work out that if #7 had 1000mL in the sustain chamber like #6 the end of the
sustain water phase would have been 0.48 seconds later which
almost puts it on par with where it thrust finished for test #6.
Therefore test #7 generated approximately 8 Ns more thrust
during the sustain air phase than in #6. This performance gain
should be measurable in the flight tests.
Comparison of test #6 and #7
Measuring the thrust difference in the boost phase with and
without blow-through is
difficult to do with our current setup due to how short the
phase is. The boost phase water and air last about ~0.25 seconds. We sample the load cell at only 240Hz
and due to the initial launch upward kick, the rocket briefly
oscillates on the load cell so we get quite noisy data during
the first 0.1seconds of the launch. How effective the no
blow-trough boost actually is will be done during flight trials.
Here are some video frame captures from the tests:
Looking at the boost phase
There is no blow-through during
the boost phase
With the o-ring removed you can
see
some spray from the inlet holes.
Looking at the spacer sustain
phase
with collapsed bottle
Another view of the
collapsed bottle
Start of boost
air pulse
Dramatic bottle collapse during
the spacer sustain phase
Video
Here is a highlights video from
the tests:
Water Self-Levelling
The one problem encountered during the load cell tests was that the water self-levelling
didn't quite work as well as expected. This was traced to pressurised air entering the extension tube directly from the
release head, preventing a large enough pressure differential
between the sustain chamber and the boost chamber. The pressure
differential is important in order to force the water into the
sustain chamber.
In test #7 we poured some of the water into the sustain chamber
beforehand to help distribute the water better.
Self-Levelling Tests - 1/1/2014
After a short break for Christmas and New Year we followed up
with the self-levelling tests.
Test #
Configuration
Water amount
(mL)
Split
Boost / Sustain
( mL / mL)
Pressure
(psi / bar)
Nozzle
Boost / Sustain (mm)
Notes
1
Extension
1800
400 / 1400
50 / 3.4
22 / 5
Bypass tube causes too much water to transfer.
2
Extension
1800
900 / 900
100 / 6.9
22 / 5
Bypass tube with plugged extension tube.
The first attempt at fixing this issue was to add a small
flexible tube to the release head that bypassed the bottom of
the extension tube so that all the air would go into the boost
chamber. The first trial showed that only very little water and
air went through the non-return valve mostly because the hole in
the extension tube offered much less resistance than the
non-return valve. This makes sense because the holes in the
non-return valve are small and the o-ring provides some amount
of resistance. With most of the water going through the
extension tube this meant that most of the water was pushed up
into the sustain chamber.
We then took a skewer stick and wrapped some electrical tape
around it to fit into the extension tube. This acted as a
plug to prevent water being forced
through it and allow it to flow through the non-return valve.
The plug just gets ejected during launch. It could be
permanently attached to the inside of the release head. This did the trick and allowed the non-return valve to
do its work and correctly self-level the water in the two
pressure chambers.
Too much air entering the
extension tube directly prevents correct
water self-levelling
Using a thin
bypass tube to prevent air
entering the
extension tube.
The bypass tube allowed too much
water to flow
up through
extension tube.
Plugging
the
extension
tube prevented water
flowing up through it allowing
it to flow through
the non-return valve.
This achieved
the correct
self-levelling
operation.
Other Observations
During test #4 when we reached about 30psi the rocket self
released. Review of the video showed that the released head
collar wasn't pushed all the way up and the tops of the cable
ties were showing.
During test #5 the release head impacted with the
deflection brick and
snapped the Gardena adaptor. So we switched to our second
identical Clark
cable-tie launcher for the remainder of the tests.
During the
boost phase it was evident in the slow motion video that the
extension tube moved around quite a bit from side to side, but during the sustain
phase it was nice and steady. It should be possible to put
little flat brackets on the end of the tube that sit just above
the release head to help steady it during flight, but this may
not be necessary. The brackets would be directly in the water
flow and cause extra resistance.
During correct self-levelling the water always settles a
little bit below the non-return valve. This is because the
bubbles coming up through the water increase its volume
raising the water level. When the bubbles stop, the water
level drops.
Conclusions
The extension tube prevents the blow-through effect and
allows the water to be ejected cleanly from the boost chamber.
The extension tube also prevents the vacuum forming in the boost
chamber during the sustain air pulse. The sustain air pulse
also generated an additional 8Ns of thrust in these tests. With
the extension tube plugged in the launcher, the non-return valve
works well to self-level the water in the boost and sustain
chambers.
Next will come a series of flights with this new arrangement
to see how it performs.